Nothing much, but here you can actually see the twins.
I have now replaced the single 120mm 6000 rpm fan with twin 80mm 13000 rpm fans.
You cannot see them in this video clip, but you can certainly hear them.
The twin fan setup is a lot more efficient then the single fan. Full load temperature dropped somewhere around 7 deg. C, and that’s a lot. Also; it may be a bit hard to see on my messy work bench, but I have now modified the OP-amp circuits on the LED Audio VU meters, and they now shows forward and reflected power.(they are on the desk just in front of the pa-deck)
By the way, here finishing a QSO via the moon with DK4RC.
Here is a Saturday morning update report regarding my rf switch project.
Back to the good old drawing board, I guess.
Switch are switching ok, and loses are acceptable, this is fine.
However, it is picking up ambient noise. I suspect its being a shielding problem and an isolation problem between RF parts and DC parts of the relays.
To give you an idea of the rx degradation with this thing is in line compared to the narda 023.
Pointing the 144 array to a relatively cold spot, the wsjt noise floor rises about 4dB, and this is simply not acceptable. This thing is useless for weak signal work until these problems are rectified.
I have now installed a narda 023 again.
Hoping to do some EME contacts again this weekend. See you on the moon.
Morning report: Saturday 25.03.2017, still messing around with my quest for low cost high power rf-switch. I have cut and soldered a lot-lot-lot-lot-lot of coaxes since last post and….. Well, now it is looking really good, I have exchanged all the small diameter coaxes with larger ones, and there are now no heat loss I can feel with my fingers!
Operator is a bit too eager going on with the testing here, not checking all connection beforehand, resulting in the SSPA safety system trigging several times before it get going. (shame on me)
Here are a some pix & unabridged videos:
Been quite busy experimenting with this rf-switch the last couple of days.
There has arrived a lot on and off-list comments regarding rf-switches and I have not had the time to answer all, but thanks.
I am now up in what I call revision 4 switch.
Revised schematics for better RX/bypass-port isolation.
New 10 amps relays.
Have done a lot of λ/4 coax tuning.
TX loss is slightly better.
RX loss is slightly worse.
RX isolation is much better.
What needs to be done:
Switch works but the 75 ohm rg-179 stubs are getting way to hot when passing the Kw level.
Need to find something better.
I have got some questions about the home brew rf-switch or relay in my previous post.
To clarify, I got this idea from Leif, sm5bsz web site.
He has done this with PIN-diodes. I don’t have suitable diodes on stock here so I substituted those with small relays. Problem is that lo-Z current at the relays are way to large, and I got to do something with that. Upgrading to larger relays would only make the Q higher and move the problem over to the coax subs I guess. I think. What is needed, is to lower the Q, maybe by adding a small resistor at the relays, say for example 0.1 ohm. (at the point of writing this, I must emphasize, I have not done the math yet.) But I have a feeling it my work. We will see……… 🙂
UPDATE: I have now done the math, and installing a series resistor at the lo-Z point will not lower the rf-current. It will only increase insertion loss. RF-current is about 4,2 amps, and my small signal relays are rated 2 amps @ 30VDC, Guess I got to find some larger ones.
Hi guys, I have an update regarding my mosfet troubles. To keep the story short……….:
Last weekend I got the replacement mosfet, I installed it, SUCCESS!!! According to its markings, it was a couple of years older than the other one, and it needed abt. 0.5 volt higher bias voltage, but this is fine once adjusted.
Then I started testing again, this time with a more mature swr protection system, this system tripped immediately. Hmmmmm. What could be wrong???
OK, fast forward, back to the time of breakdown event: It was a late weekend evening. The operator may have been a bit tired, eager to produce some results. There may have been a couple of beer cans in the way. 🙂 And the shack do not look good in daylight… this does not help at midnight, but it may appear better, visually.
I am now, pretty sure that the cause of the mosfet breakdown was a missing load, not spikes or over drive from the driver. Looking for the cause for the high swr situation mentions above, I found that the TX relay (narda 023 series) had a short due to internal welding!!!! Also, the coax connected to the transmitter port had a short. The RG-142 Teflon center insulator had developed a puncture, shorting it out!!!!! There have been some serious voltage on the loose here.
Well. I repaired the relay and exchanged the damaged coax. Up and running again, but not for long. A piece of advice; knowing about their internals, relays like the narda 023s, do not abuse them. They are high cost, wide band, low insertion loss, high power relays, but keep them below the rated power limit. I think these are rated to at abt. 1Kw @ 100 MHZ @ low vswrs conditions. Well, I tested it for key down, 2Kw at 3 minutes and it would not operate any more. Wye?? Because the internal plastic bits has melted and permanently deformed.
Looking for a better replacement I discovered that an electromechanically solution does not in practice exist at these power levels. Not what my wallet is going to accept any way.
Then I come to think of SM5BSZ Leifs page, about High Power PIN Diode Switch. Well, I do not have suitable PIN diodes, but I have many different relays. Let’s try that instead. …….And it works. Only trouble is that my Q is to high. RF-current melt the solder and things broke down……again. But this can easily be rectified.
……..to be continued……….
……here are some pix.
Video above show the first run with the new switch. It broke down, but this time the mosfet protection works.
Last night, during light burn-in tests, the amplifier suddenly dropped gain.
No alarms, no nothing, but one of the MOSFETS was drawing a lot less current compared to the other, it was also operating in class C. It turns out that for some reason the gate2 on the failing MOSFET has broken down. DAMN!!!!!!!!
Some more SSPA development stuff.
Sorry for the low word count.
But then again, here are some videos 🙂